Initialising ...
Initialising ...
Initialising ...
Initialising ...
Initialising ...
Initialising ...
Initialising ...
Saito, Kazuo*; Ishida, Toshihisa
JAERI-Tech 2001-039, 25 Pages, 2001/06
no abstracts in English
*; *
PNC TJ9381 94-001, 84 Pages, 1994/02
The study in last year examined the realization of 1000MWt natural circulation ATR. In this study. The sensitivity analysis is did making for the design. The results are as below. (1)The influence of riser pipe diameter. The natural circulation on riser pipe 3B is analyzed. 3B pipe is cheaper than 5B riser pipe that is a base condition. The results are that fuel dryout is happen by 1.8MW channel power on 3B, but is not happen on 5B riser pipe. (2)The influence of the riser pipe number reduction and the riser pipe diameter change. The case of connection 2 pressure tubes by Y piece pipe is analyzed. In this case, the riser pipe number is half. The cases that riser pipe is 5B and 4B are analyzed. The results are as below. (a)Natural circulation flow lower by riser pipe number is half. (b)Fuel dryout is happen by 1.8MW channel power on 4B, but is not happen on 5B. (3)The influence of the middle position header connection and the riser pipe diameter change, The case of connection 50 pressure tubes by the middle position header is analysed. The cases that riser pipe is 24B and 32B are analyzed. The results are as below. (a)In 2 cases, natural circulation flow lower as compared with base case. (b)In 2 cases, fuel dryout are not happen by 1.8MW channel power. (4)The influence of pressure tube diameter. The case of pressure tube diameter widening is analyzed. So, the pressure loss of pressure tube domain govern the flow. (a)Natural circulation flow increase by pressure tube diameter widening. (b)The flow swing is by pressure tube diameter widening. (c)In analysis cases, fuel dryout is not happen. We get 1.8MW channel power on the condition that riser pipe is 4B, riser pipe is connected by Y piece pipe, pressure tube diameter is 122.0mm.